Drove over to my uncle in laws to trouble shoot with a mechanically inclined partner. Please GMSB keep in mind I don't know as much as I want to about this truck and it's TBI system as I want to, and my uncle in law doesn't either.
When I got there we tested the battery in DC and it tested good at 12.6 volts. We turn the truck on and the battery voltage jumped up to 14.9, as in, the alternator is doing it's job. So then the test drive.
He rode with me and experienced the rough ride and stuttering. He mentioned thinking it could be fuel related. We talked about the fuel pump, the missed fuel pressure test( I could not seem to ever thread the TBI specific port fixture to the flex line a while ago and abandoned the test). So he suggested maybe the tank wasn't venting properly so he suggested trying to drive it with the gas cap off. It maybe ran rougher after that, so we put the cap back on and headed back to his house, only after the truck cut out on us when I put it in reverse to turn around. We made it back to his house and he brought out a vacuum test. We tried hooking it up in the ports on the canister, with no pressure change, leading me to believe the canister system may be deleted on this truck or just dead old.
Then we started looking for ports to test pressure in and around the throttle body. I explained to him what all the electronic sensors were. He started unplugging and plugging back in on: PCV(pressure shot out immediately and engine revved, once re-plugged the engine settled and smoothed out), The EGR(nothing happened???), the MAP sensor(again, pressure shot out, engine revved, plugged back and engine settled, and smoothed out). After this the engine was idling much smoother than before we started tinkering with the ports on the TBI. He wished me luck and we talked about changing spark plug wires potentially and replacing the EGR(which I have never done) in the next few days.
I put the truck in reverse to leave and it had plenty of power. Put in drive to head home and the truck had all the power it normally should. It is currently driving like nothing is wrong. So strange. All I can think is it had something clogged in the EGR(or one of the other ports maybe) and when we messed with them something got knocked out or unclogged. SMH.