The_Fry_Lord
Junior Member
- Joined
- Jul 5, 2024
- Posts
- 4
- Reaction score
- 2
- Location
- British Columbia, Canada
- First Name
- Cody
- Truck Year
- 1979
- Truck Model
- K10
- Engine Size
- 350
Hey! New to posting on here but been somewhat of a lurker in recent months reading posts. I see that diagnosing gauges is a relatively common thing for these GM squarebody trucks, and was wondering if someone could assist me. I have had issues with my oil pressure gauge for a while, I have replaced both the gauge, and the sending unit. Additionally my truck has a brand new painless wiring kit, every single component of the system is brand new. Gauge, wiring, cluster circuit board, sending unit. Yet I am still having issues with the gauge.
The gauge works, but is not accurate. Around 30PSI and below it reads accurate, above 30PSI it is increasingly inaccurate the higher my pressure is. The sending unit is rated for 95ohm resistance @ 60PSI and above, and this has been bench tested. Results of the bench test are as follows;
60PSI - 95ohm
45PSI - 80ohm
30PSI - 56ohm
15PSI - 27ohm
10PSI - 21ohm
5PSI - 3ohm
0PSI - 3ohm
My old oil pressure gauge utilized an external resistor, and my new gauge uses an internal resistor. Old gauge had the white block between terminals on the back of the guge with a small printed circuit for the electrical path, new one does not its just a piece of plastic to fill space. Tested the new gauge, and it reads 70ohm resistance. I have not tested the old gauge resistor yet. However, the old gauge was working good at one point, both before and after I installed the painless wiring kit. Grounding shouldnt be an issue as the sender grounds through a brass fitting and then into my manifold, and the whole engine is grounded via a braided 1" wide ground strap bolted directly from the head on the engine to my frame.
So, my sender range is 3-95ohm, and my gauge is internally resisted at 70ohms. What have I done wrong, or what do you think I need to do to get these to work? Individually they both work but it seems my issue lies with communication between the sender and my gauge. I am going to build some test leads for my old gauge, and hook it up to the sender while its on the tester so I can increase pressure to the sender via my test kit while watching how the gauge reacts.
Wanted to make a post here incase anybody had ideas, I am experiencing a similar issue with my fuel gauge as well but it is always maxed whereas with my oil pressure gauge, it does move with the pressure, just reads way too high when my PSI is above 30. From wha I understand, the gauge has to match the sender, so if I have a 95ohm sender I should have a 95ohm gauge. But, I cannot change the resistor on my new gauge as its internal. Hopefully I can get some advice from everybody here who knows far more about it than I do.
Thanks everybody!
The gauge works, but is not accurate. Around 30PSI and below it reads accurate, above 30PSI it is increasingly inaccurate the higher my pressure is. The sending unit is rated for 95ohm resistance @ 60PSI and above, and this has been bench tested. Results of the bench test are as follows;
60PSI - 95ohm
45PSI - 80ohm
30PSI - 56ohm
15PSI - 27ohm
10PSI - 21ohm
5PSI - 3ohm
0PSI - 3ohm
My old oil pressure gauge utilized an external resistor, and my new gauge uses an internal resistor. Old gauge had the white block between terminals on the back of the guge with a small printed circuit for the electrical path, new one does not its just a piece of plastic to fill space. Tested the new gauge, and it reads 70ohm resistance. I have not tested the old gauge resistor yet. However, the old gauge was working good at one point, both before and after I installed the painless wiring kit. Grounding shouldnt be an issue as the sender grounds through a brass fitting and then into my manifold, and the whole engine is grounded via a braided 1" wide ground strap bolted directly from the head on the engine to my frame.
So, my sender range is 3-95ohm, and my gauge is internally resisted at 70ohms. What have I done wrong, or what do you think I need to do to get these to work? Individually they both work but it seems my issue lies with communication between the sender and my gauge. I am going to build some test leads for my old gauge, and hook it up to the sender while its on the tester so I can increase pressure to the sender via my test kit while watching how the gauge reacts.
Wanted to make a post here incase anybody had ideas, I am experiencing a similar issue with my fuel gauge as well but it is always maxed whereas with my oil pressure gauge, it does move with the pressure, just reads way too high when my PSI is above 30. From wha I understand, the gauge has to match the sender, so if I have a 95ohm sender I should have a 95ohm gauge. But, I cannot change the resistor on my new gauge as its internal. Hopefully I can get some advice from everybody here who knows far more about it than I do.
Thanks everybody!